求解 收敛问题 the damping factor(阻尼因子)太小怎么办,
这个是message里的内容READING PRO/II DATABASE
PROJECT USER
PROBLEM DATE
*** PROBLEM SOLUTION BEGINS
FEED FLASH BEGINS
FEED FLASH COMPLETE
UNIT 1 BEGINS - 'T1 '
INNER0 : E(ENTH+SPEC) = 2.265E-01
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 2.258E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 2.258E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 2.091E-01ALPHA = -0.0012
INNER4 : E(ENTH+SPEC) = 2.037E-01ALPHA = -0.0009
ITER1 E(K) = 1.593E-01 E(ENTH+SPEC) = 2.037E-01E(SUM) = 8.417E+00
DAMP = 1.000E+00
INNER0 : E(ENTH+SPEC) = 1.829E-01
INNER1 : E(ENTH+SPEC) = 1.675E-01ALPHA = -0.0016
INNER2 : E(ENTH+SPEC) = 1.659E-01ALPHA =0.0001
INNER3 : E(ENTH+SPEC) = 1.655E-01ALPHA = -0.0009
INNER4 : E(ENTH+SPEC) = 1.616E-01ALPHA = -0.0001
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.602E-01ALPHA =0.0020
INNER2 : E(ENTH+SPEC) = 1.600E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.595E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.595E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.595E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.595E-01ALPHA =0.0000
CALCULATING NEW MATRIX
INNER1 : E(ENTH+SPEC) = 1.595E-01ALPHA =0.0000
INNER2 : E(ENTH+SPEC) = 1.595E-01ALPHA =0.0000
INNER3 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
INNER4 : E(ENTH+SPEC) = 1.596E-01ALPHA =0.0000
*** ERROR ***COLUMN calculations TERMINATED. Alpha ( the damping factor )
was BELOW .01 for 4 consecutive iterations after 15 new matrix
calculations.
*** A FATAL ERROR OCCURRED ON ITERATION 2
*** ERROR HISTORY IS NOT AVAILABLE FOR THIS ITERATION
UNIT 1 NOT SOLVED
*** PROBLEM SOLUTION NOT REACHED
*** Run completed - Case not solved
*** THIS RUN USED 2.00 PRO/II SIMULATION UNITS
*** RUN STATISTICS
STARTED 10:15:00 04/28/11 1 ERROR
FINISHED 10:15:03 04/28/11 NO WARNINGS
RUN TIMES NO MESSAGES
INTERACTIVE 0 MIN,0.00 SEC
CALCULATIONS 0 MIN,2.17 SEC
TOTAL 0 MIN,2.17 SEC
进来就是看看.................... 这个。。。太复杂了,没看懂。。 不明物体 看不懂 en ,我也曾遇到过类似的问题,不过通过调整塔板数,采出量,以及进料为止,
最后就收敛了。
你自己再改改参数调调试试
页:
[1]