|

楼主 |
发表于 1970-1-1 08:00:00
显示全部楼层
下面是模拟结果,气相:SO2 58m3/h,N2 32226M3/H,温度 293K,压力101KPA. 液相:30%的氢氧化钠溶液150m3/h,温度 293K,压力104KPA
塔板数:15. 拉西环填料
顺便问一下,aspen能否直接计算填料高度,就像简捷法计算塔板数一样。现在用的是先估算塔板数,再根据塔板数与填料的等量高度,计算填料高度。实际中我若是能够估算准塔板数,就不用aspen计算了!
->Calculations begin ...
** ERROR
RADFRAC NOT CONVERGED IN 25 OUTSIDE LOOP ITERATIONS.
*** SEVERE ERROR
MATERIAL AND ENERGY BALANCES FAILED TO CONVERGE: CHECK COL-SPECS
OR SUPPLY BETTER TEMPERATURE AND COMPOSITION ESTIMATES.
* WARNING IN PHYSICAL PROPERTY SYSTEM
ATTEMPT TO USE MODEL ELECNRTL WITHOUT A SOLVENT.
ACTIVITY COEFFICIENT OF UNITY IS USED
* WARNING IN PHYSICAL PROPERTY SYSTEM
ATTEMPT TO USE THE CLARKE AQUEOUS ELECTROLYTE DENSITY MODEL
WITHOUT A SOLVENT. CALCULATION NOT PERFORMED.
* WARNING IN PHYSICAL PROPERTY SYSTEM
ATTEMPT TO USE THE CLARKE AQUEOUS ELECTROLYTE DENSITY MODEL
WITHOUT A SOLVENT. CALCULATION NOT PERFORMED.
** ERROR
H-LOOP DOES NOT CONVERGE IN 5 TRIALS. ENERGY BALANCE NOT SATISFIED
WITHIN MAXIMUM NUMBER OF ITERATIONS.
** ERROR
FLOODING CALCULATIONS FOR SECTION (1) FAILED TO CONVERGE.
CALCULATED DIAMETER MAY NOT BE ACCURATE.
** ERROR
PRESSURE DROP CALCULATIONS FAILED TO CONVERGE. PRESSURE DROP
CALCULATED FOR SECTION (1) MAY NOT BE ACCURATE.
** ERROR
BLOCK ABSORBE IS NOT IN MASS BALANCE:
MASS INLET FLOW = 0.48206959E+04, MASS OUTLET FLOW = 0.48044435E+04
RELATIVE DIFFERENCE = 0.33827761E-02
* WARNING
STREAM NAOH IS NOT IN CHARGE BALANCE:
ANION FLOW = -.50342386E+00, CATION FLOW = 0.51602005E+00
RELATIVE DIFFERENCE = 0.25021041E-01
* WARNING
STREAM W IS NOT IN CHARGE BALANCE:
ANION FLOW = -.67645052E+01, CATION FLOW = 0.95116797E+01
RELATIVE DIFFERENCE = 0.40611611E+00
->Simulation calculations completed ...
*** SEVERE ERROR
FORTRAN OVERFLOW ENCOUNTERED.
** ERROR
FLOODING CALCULATIONS FOR SECTION (1) FAILED TO CONVERGE.
CALCULATED DIAMETER MAY NOT BE ACCURATE.
** ERROR
PRESSURE DROP CALCULATIONS FAILED TO CONVERGE. PRESSURE DROP
CALCULATED FOR SECTION (1) MAY NOT BE ACCURATE.
* WARNING
VLSTD MISSING FOR COMPONENT SODIU(S).
CALCULATED STDVOL FLOW WILL BE INCORRECT.
*** SEVERE ERROR
FORTRAN INVALID OPERATION ENCOUNTERED.
Convergence iterations:
OL ML IL Err/Tol
1 1 1 0.24254E-09
2 1 1 0.23979E-09
3 1 1 0.94145E-11
*** SEVERE ERROR
MATERIAL AND ENERGY BALANCES FAILED TO CONVERGE: CHECK COL-SPECS
OR SUPPLY BETTER TEMPERATURE AND COMPOSITION ESTIMATES.
*** SEVERE ERROR
THE FOLLOWING STAGES DRIED UP:
13
A LIMIT OF 0.10000E-04 * SUM OF FEEDS WAS IMPOSED ON THE FLOW RATES.
* WARNING IN PHYSICAL PROPERTY SYSTEM
ATTEMPT TO USE MODEL ELECNRTL WITHOUT A SOLVENT.
ACTIVITY COEFFICIENT OF UNITY IS USED
* WARNING IN PHYSICAL PROPERTY SYSTEM
ATTEMPT TO USE THE CLARKE AQUEOUS ELECTROLYTE DENSITY MODEL
WITHOUT A SOLVENT. CALCULATION NOT PERFORMED.
* WARNING IN PHYSICAL PROPERTY SYSTEM
ATTEMPT TO USE THE CLARKE AQUEOUS ELECTROLYTE DENSITY MODEL
WITHOUT A SOLVENT. CALCULATION NOT PERFORMED.
** ERROR
H-LOOP DOES NOT CONVERGE IN 5 TRIALS. ENERGY BALANCE NOT SATISFIED
WITHIN MAXIMUM NUMBER OF ITERATIONS.
** ERROR
BLOCK ABSORBE IS NOT IN MASS BALANCE:
MASS INLET FLOW = 0.48206959E+04, MASS OUTLET FLOW = 0.12609178E+08
RELATIVE DIFFERENCE = 0.26146345E+04
* WARNING
STREAM NAOH IS NOT IN CHARGE BALANCE:
ANION FLOW = -.50342386E+00, CATION FLOW = 0.51602005E+00
RELATIVE DIFFERENCE = 0.25021041E-01
* WARNING
STREAM W IS NOT IN CHARGE BALANCE:
ANION FLOW = -.67644409E+01, CATION FLOW = 0.95115894E+01
RELATIVE DIFFERENCE = 0.40611611E+00
->Simulation calculations completed ...
<< Loading Simulation Engine 20:45:55 Thu Aug 11, 2011>>
->Generating report ... |
|